Analisis Kinerja Kompressor Screw Oil Injected Sullair Ls20-150h untuk Ash Handling (Study Kasus PLTU Teluk Sirih)
DOI:
https://doi.org/10.31004/jutin.v7i1.25494Keywords:
Compessor, Ash, air pressure, DustAbstract
PLTU Teluk Sirih is a coal-fired steam power plant as an energy source that produces ash with a capacity of 2 . The compressor is a medium for transferring ash by using compressed air. The compressor used is a SCREEW OIL INJECTED SULLAIR LS20-150H compressor. Currently there is a decrease in performance on the compressor, which initially had a compression ratio of 1,600 Psia, polytropic head 14,500,599, capacity 10,938,438, flow rate 11,379,622 lb/s, efficiency 98.5%. After analyzing this compressor, the data obtained was a compression ratio of 1,540 Psia, polytropic head 13,805,166, capacity 10,950,733, flow rate 11,392,412, and efficiency of 95.3%. The reason is because the compressor room area does not have an active blower so that dirt/ash stuck to the radiator fins causes heat transfer to be hampered and this greatly affects the performance of the compressor parts to work optimallyReferences
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